|
|
![]() |
#1 |
Banned
Join Date: Feb 2008
Posts: 852
Likes: 0
Liked 0 Times in 0 Posts
|
![]() |
![]() |
![]() |
![]() |
#2 |
Member
Join Date: Dec 2011
Location: Indiana
Posts: 437
Likes: 15
Liked 18 Times in 6 Posts
|
![]()
I thought the issue lied with the chamber design not being as FI friendly causing pre-ignition taking out the head gaskets. I don't have much experience with FI LSs through because they ran so well NA on and off nitrous and had no room to stuff a blower/turbo under the hood of the GM cars.
Is there head warpage issues? The early B-head 4 valve modulars had that issue with some mileage on them. Both the cars use MLS gaskets so that would make sense.
__________________
2014 Cobra Jet FS/XX #3345 STK/SS Like us on http://www.facebook.com/pages/Daniel...25886327426822 |
![]() |
![]() |
![]() |
#3 |
Senior Member
Join Date: Oct 2003
Location: usa
Posts: 958
Likes: 0
Liked 0 Times in 0 Posts
|
![]()
D John , you got it correct
__________________
Bo Kenney |
![]() |
![]() |
![]() |
#4 |
Banned
Join Date: Feb 2008
Posts: 852
Likes: 0
Liked 0 Times in 0 Posts
|
![]()
The chamber design leaves a lot to be desired, but the casting bending under cylinder pressure is a major issues. I know this is different but the Dura Max has same problem when the cals are changed.
|
![]() |
![]() |
![]() |
#5 |
Veteran Member
Join Date: Mar 2005
Location: Sand Springs, OK
Posts: 8,132
Likes: 896
Liked 390 Times in 170 Posts
|
![]()
Pretty much what we found. One customer (not real sharp) had his block & heafs machined for 5/8" studs. He had a turbo with a lot of boost. All he accomplished was more block and head deck distortion when he torqued them. Actually pushed gaskets out sooner. Tried to tell him, but he was still in his 20s. I remember being in my 20s. Life was simpler when I has all the answers. LOL
__________________
Ed Wright 4156 SS/JA |
![]() |
![]() |
![]() |
|
|