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#21 |
Member
Join Date: Aug 2003
Location: Atlanta
Posts: 476
Likes: 20
Liked 70 Times in 22 Posts
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Glad you solved the problem. Wanted to share this 833 4speed story but not until your problem was solved.
Had a 4speed 68 dart that worked fine, then it started not going into 2nd above 4000. Normal cruising it was fine. I pulled it and looked it over and couldn't see anything. Put it back in the car with no change. Pulled it again, this tore it all the way down, found nothing, put it together and back in and still didn't work. This was 40+ years ago when I thought you could get lucky and just by taking it apart and putting it back magic would fix it. I've lost that belief. Tore it apart again and just happened to pull on the brass syncro ring and it spread. It was split thru in one spot and above 4000 it would open up enough not to fit as it should.
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Stewart Way 2424 SS |
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#22 |
VIP Member
Join Date: Apr 2005
Location: Greensboro NC
Posts: 1,027
Likes: 1
Liked 83 Times in 32 Posts
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PM me your phone number, Ill have Herb McCandless Sr call you, he probably knows more about a Chrysler 4 speed that anyone around.
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#23 | |
Member
Join Date: Jan 2010
Location: Minnesota
Posts: 409
Likes: 0
Liked 0 Times in 0 Posts
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Jerry Williams NSS/A, E/S, PRO E.T. And the "Grandaddy" of Gen III Hemi Performance...The fire inside me still burn's. |
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#24 |
Member
Join Date: Jan 2010
Location: Minnesota
Posts: 409
Likes: 0
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Thanks for the offer. Are you Herb's son? I just built a motor using Herb's new set of spare 440 .060" over Venolia piston's from his 69 Bee. I plan on asking Herb to signature the box at this year's Mopars in the Park in MN.
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Jerry Williams NSS/A, E/S, PRO E.T. And the "Grandaddy" of Gen III Hemi Performance...The fire inside me still burn's. |
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