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#1 |
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I keep killing the thrust bearing in my 360 Stocker after 10 passes.
Last time, had the thrust repaired on the crank, freshen the convertor, changed to another 904 trans, did away with the quik disconnects on the trans cooling lines. After the thrust repair, I had .002 endplay. The time before, had .010 endplay. All the bearing look great. Anyone else have this problem? |
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#2 |
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.002 is too tight it will cause a failure.
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Lee Valentine 1661 STK |
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#3 |
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I agree with Lee,that is rather snug. Out of curiosity,what is your stall
speed? I have seen a real high rpm stall causing early thrust brg. problems but I would think a stocker wouldn't hit all that hard. All your end play etc is within specs I assume. Good luck devo |
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#4 | |
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Jim Carter 2340 Super Stock 2340 SST/2340 Stock Set another place at the table Last edited by jmcarter; 09-09-2017 at 06:39 PM. |
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#5 |
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I though .002 might be too tight, I checked the service manual & it had .002-.010 for range.
It is a ATI convertor, sent it back to them. Asked about it ballooning, no concerns found. It was freshened up at that time also. It is footbraked to 3K to leave. Another racer was having the same problem with a 340 Stocker. He recommended me to a guy at Pro Trans. They have a piece called the "destructor" that goes into the convertor charge hole. I haven't disassembled the engine from this last failure to inspect the bearing yet. Just cut the oil filter open, found bearing material & the crank has excess movement. I checked the crank during the last race, it didn't kill it until the last two passes. Also lost a tenth at the same time. |
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#6 |
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0.002" is way too tight for a race engine.
0.007" is more typical for a race engine. I lot of flexing occurs under the high stresses in a race engine. Also, please check the end play with JUST the upper bearing in place, then again with JUST the lower bearing in place to confirm the alignment of the upper to lower bearing halves. You know the saying, "If you have too much bearing clearance you are the only one who knows. If you don't have enough bearing clearance, EVERYBODY knows." It's best that you are the only one who knows. |
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#7 |
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Devo,
Is this a new engine or has it run before without hurting the thrust bearing ? The reason I ask is I had a problem with a thrust bearing in a 350 Chevy years ago. The block had been align honed and when they cut the cap they cut it crooked and it was tilting the thrust bearing just slightly. Took me a while to figure it out. Did something change in your combination right before your thrust problem started ? Just thinking out loud ![]()
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Bill Koustenis |
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#8 | |
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#9 |
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do you have another transmission you can test with?
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#10 |
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Are both the dowel pins that align the bellhousing still in the block . Sounds like something didn't go back together the same after the trans repair .
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